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投稿时间:2019-08-22 修订日期:2019-09-10
投稿时间:2019-08-22 修订日期:2019-09-10
中文摘要: 铜坑矿92#矿体采用空场嗣后废石充填法、组合崩落法进行开采,由于采空区治理不及时、不彻底,预留的盘区柱在高水平应力作用下片帮、冒顶,成为难采孤岛破裂矿柱。文章以201#线孤岛破裂盘区柱为试验采场,通过开展岩石完整性测试,评价采场底部结构的稳定性,采用数值模拟方法对盘区柱破裂演化规律进行分析,评价破裂矿柱诱导崩落可行性,并运用部分空场—诱导崩落法联合回采,实现破裂矿柱诱导崩落,试验采场贫化率由29.4%降低至17.5%,损失率由43.8%降低至26.3%,取得良好的安全生产效果,为其它类似开采条件的破裂矿柱回采提供技术参考。
Abstract:Open stoping with subsequent rock filling method and composite caving mining method are used for the mining of No. 92# ore body of Tongkeng Mine. For lack of timely and thorough treatment of goaf, rib spalling and roof fall often occur in the reserved panel columns for high horizontal stress,and many isolated fractured pillars have been formed. In this paper, the 201# line island rupture zone column is used as the test stope. The rock integrity test is carried out to evaluate the stability of the bottom structure of the stope. The numerical simulation method is used to analyze the rupture evolution law of the block column and evaluate the fracture column induction. Feasibility of caving, and the use of partial empty field-induced caving method combined mining, to achieve the collapse of the collapsed pillar. The dilution rate of test stope was reduced from 29.4% to 17.5%, and the loss rate was reduced from 43.8% to 26.3%. Good safety production effect was achieved. It provides technical reference for other fractured pillar mining under similar mining conditions.
文章编号:20190822001 中图分类号:TD852 文献标志码:
基金项目:
作者 | 单位 | 邮编 |
潘桂海* | 北京矿冶科技集团有限公司 | 100160 |
王湖鑫 | 北京矿冶科技集团有限公司 | 100160 |
于世波 | 北京矿冶科技集团有限公司 | 100160 |
何晓武 | 广西华锡集团股份有限公司铜坑矿 | 547207 |
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